I was
very lucky to be able to buy an
keyboard from someone in
in non-working order as a renovation project and it
gave me the opportunity of owning and playing this classic British synthesizer.
A friend and fellow
In these pages I will describe the project with a hope
that it will provide useful info for those people who already own VCs3’s/synthi
A’s and whose units might suffer from some of the problems my unit had. Anyway
if you have always wanted to see the insides of a vCS3 here we go!
First up here are some pics of the unit I
bought..(AFTER making some cosmetic repairs!)




The
pics above show the unit after I had worked on the cosmetics a bit. When I
first got it ..it was pretty dirty and needed a good clean. It looked a whole
lot better after that..and I could see what things needed repair.
Woodwork Repairs
The wooden case on the VCS3 is really pretty to look
at ..and gives the synth its unique styling.
The wood is quite exotic..`aformosia’ as I understand.
Anyway it’s a skilled job to make one of these cases ..mortice and tennon
joints everywhere and angles to get right. The case on mine had suffered a bit
with most of the joints needing re-gluing. This was the first thing I
did..using wood glue to reset all the joints. There was a small crack along one
side, near the point where the speaker holes are located. This is a well known
weak point on VCS3’s so I wasn’t too surprised to find one. Carefully opening
the crack slightly and inserting gluing, its possible to get an almost
invisible repair.
After re-seting the joints..the whole unit become very
solid. Only fiddly part was getting
the front panels to fit into the slots that hold them
in place..but eventually I did it.
The major woodwork repair was yet to come! The unit
had lost its wood top piece at some point in the past but luckily Greg (the
person I bought it from) had obtained a piece of bare wood (aformosia?) that
was a very close match to the existing woodwork. This came with the synth as a
cut rectangular block. The task remained to cut this as precisely as possible,
with the correct angles to fit perfectly onto the joints on the top of the
vertical sides of the unit.
I did this ok..what remained was to route out the
slots for the joints and two long thin slots
which take the front aluminium panel and the rear wood
panel. I found this a bit tricky..but using a drill press with a router bit
finally got the job done in a day. The results are pretty good to look at. The
new wooden top blends in very well with the existing wood.
Next I wanted to re-finish the lovely aformosia! There
were a number of scratches/scuffs etc on the wood that is typical of use over
25 years. Using very fine wirewool ..I gently removed the old finish and with
it these scratches. There remain a couple of dings here and there which will
require attention ..but these could wait until I got the synth working.
When I finally got the finish I wanted..I then decided
I wanted an oil satin-sheen finish on the wood. A good oil to use is tung-oil
based ‘Antique Oil’. The technique to getting a satin smooth finish with oil
depends on the wood you are working with. The bare aformosia has some open
grain
which would normally prevent satin finishes with oil.
To remedy this ..I worked the oil into the wood using the very fine wire wool.
The idea is to produce a paste between the oil and the fine woodust that fills
any remaining open grains. After several coates of oil (leaving 1 hour between
each coat) I got an excellent satin sheen on the wood..Great!

Some of the
silver coloured knobcaps were scratched so rather than replace the whole knob
I used
some of the caps I had on the knobs I bought for my synthi
A project. I had often wondered
whether
these knobs (made by CLIFF COMPONENTS
in the
To remove
the caps you need to drop the knob in hot water..wait a couple of minutes and
then the glue softens enough so you can prise the cap off (carefully) with a
modelling knife. A quick switch over of the caps and regluing them gives you a
set of pristine silver knobs.
The
coloured ones would be more tricky ..as Cliff don’t make them anymore. Luckily
those on my VCS3 are in pretty good nick.
OK having
sorted out most of the cosmetics (and certainly the VCVS3 looked a whole lot
better for it), time to figure out what was working and what wasn’t ...
The unit powered up ok ..ie the red neon light lit up
on the front panel, but no sounds at all. First thing I checked was whether the
+12v and –9v rails were working. A quick test showed that both were faulty.
On the VCS3 there are three main circuit boards (labelled A-C) which
contain all the circuits corresponding to the various modules. Here is a quick list
of what board contains what:-
Power regulation circuit (+12/-9V )
Voltage controlled output amplifiers (channels 1+2)
Tone controls on output channels (1+2)
Voltage controlled Reverb
Envelope Shaper
Filter
Input channel amplifiers (1+2)
Ring modulator
Oscillator 1 (sine+ramp)
Oscillator 2 (square+triangle)
Oscillator 3 (square+triangle)
Noise generator and meter amplifier
Clearly the power regulator wasn’t working in my case.
After checking I found that one of the
onboard power transistors had clearly overheated in
the past and failed as the plastic transistor
socket it was mounted on had fused to the metal can! I
replaced this and a few other dead transistors (broken legs) I found on the
board. Also I replaced some electrolytic caps that were clearly leaking. After
powering up..I found I now had +12v/-9v supplies. Two cermets on Board A allow
you to trim these voltages fairly accurately. One important point to note
here..neither of the 2 metal can power transistors on board A had heatsinks on
them when I checked the board. One of them runs VERY
After repairs ..here are some pics of Board A :-
UPPER ½ OF BOARD A SHOWING HEATSINKS ON
THE TWO POWER TRANSISTORS (upper/left)
A new

photo below shows the lower
½ of Board A.

BOARD B REPAIRS
When I checked out Board B I got a bit of a surprise. The ringmodulator circuit
was not quite the classic
I had
already built one before in my synthi A clone. It’s a really nice ring
modulator. Anyway I used an AD,
This
required some pin swapping as CA3046 has different pinout from TAB101. I used a
small piece of circuit board to achieve this rather than have a mess of wires
everywhere (see photo below).
UPPER ½ of BAORD B AFTER SOME REPAIRS. NOTE THE METAL CAN
ARRAY IN THE RINGMOD section

This shows the lower ½ of BOARD B

BOARD C REPAIRS
Most of
the transistors were replaced on this board and trim pots updated to modern
closed type.
Also
supermatches transistor paits LM394CH used on all 3
This shows the upper ½ of BOARD C

This shows the lower ½ of BOARD C

This shows a view of the rear of the front panel. All the pots were
replaced with carbon type of almost exact same form factor.

This shows the view of the lower panel from below. I have since replaced
all the old electrolytic capacitors in the power supply. The reverb tank
visible below turned out to work ok..just the driver chip
